3.3 type r

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Discussion

JollyGrnMonster

Original Poster:

887 posts

198 months

Wednesday 31st July 2013
quotequote all
Massive thanks to everyone that helped out with pushing the car to the line, or swapping wheels, encouragement etc etc..

Now hooked big time and eager to run the car again and add more boost and nos smile


Simon

JollyGrnMonster

Original Poster:

887 posts

198 months

Wednesday 31st July 2013
quotequote all
Not found many video of it yet but one


http://youtu.be/l4wpKgpKJkk

JollyGrnMonster

Original Poster:

887 posts

198 months

Wednesday 31st July 2013
quotequote all

JollyGrnMonster

Original Poster:

887 posts

198 months

Sunday 4th August 2013
quotequote all
Still more to come time wise on gearchanges I think wink

JollyGrnMonster

Original Poster:

887 posts

198 months

Tuesday 6th August 2013
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Shhhhhhh I dont like an audience wink

JollyGrnMonster

Original Poster:

887 posts

198 months

Wednesday 7th August 2013
quotequote all
Filming is fine its the 30 phone calls and txts on the day asking how I got on lol

JollyGrnMonster

Original Poster:

887 posts

198 months

Wednesday 7th August 2013
quotequote all
Pmsl then I would have no work.

Just easier to not publicly say when I am running the car job done.

JollyGrnMonster

Original Poster:

887 posts

198 months

Wednesday 7th August 2013
quotequote all
Pmsl then I would have no work.

Just easier to not publicly say when I am running the car job done.

JollyGrnMonster

Original Poster:

887 posts

198 months

Monday 19th August 2013
quotequote all
Video of my fastest run at totb and carry on to a flyer run where the rear window came off at 163 oops.

Hoping to beat this before the sessions over


http://youtu.be/6lWve6poozo


Simon

JollyGrnMonster

Original Poster:

887 posts

198 months

Sunday 9th March 2014
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Dont think the 3litre is either.

JollyGrnMonster

Original Poster:

887 posts

198 months

Saturday 15th March 2014
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Rather long time since I updated this but renewed interest saw Stew @ TFS and I working on it today smile

The cars been stood for a long while whilst other stuff took priority so needs a damn good clean and tidy.
Tidied up a few bits and planned out a few jobs, amazing how you noticed stuff you never had before when you return to it after a break.
The loom is currently out the car and Ian (Bod) is currently redoing it for a syvecs s8 smile
Today the CDF fuel rails and new injectors went on - the old 960cc sidefeeds were maxxed at 1.7bar last year.

JollyGrnMonster

Original Poster:

887 posts

198 months

Saturday 15th March 2014
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Simon

JollyGrnMonster

Original Poster:

887 posts

198 months

Thursday 3rd April 2014
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Spent some time on the car today.

Servo removed


Simon

JollyGrnMonster

Original Poster:

887 posts

198 months

Friday 4th April 2014
quotequote all
At the moment straigth line only.

Next year perhaps get it out on track.

Pedal box setup correctly with correct weighted cylinders doesnt take massive effort to use.

Also the keen eye might notice I changed the turbos - gt3582r with billet wheels smile

JollyGrnMonster

Original Poster:

887 posts

198 months

Friday 4th April 2014
quotequote all
At the moment straigth line only.

Next year perhaps get it out on track.

Pedal box setup correctly with correct weighted cylinders doesnt take massive effort to use.


JollyGrnMonster

Original Poster:

887 posts

198 months

Friday 4th April 2014
quotequote all


Also the keen eye might notice I changed the turbos - gt3582r with billet wheels smile

JollyGrnMonster

Original Poster:

887 posts

198 months

Thursday 31st July 2014
quotequote all
Totb 2014 - after the successful test day on the Saturday
9.95 run on the sarturday
https://www.youtube.com/watch?v=tPpRfjsLllM

I set off to the hotel and got a needed early night leaving TFS Racing to do a couple of jobs on the car, was such a help to have their assistance all weekend.
The Sunday morning came and unfortunately the morning was spoilt by niggles on the car (cam sensor failure and the extra heat causing noise on the crank sensor, plus other little things I forget but all cost time) so lunchtime comes and goes and the cars working again, in one run to test the car where it worked I kept my foot in and the car gets very lively and weaved the whole width if the strip, the commentators reaction says it all really.

http://youtu.be/4QFQ2KqmZXs
the incar
https://www.youtube.com/watch?v=nrvVQTeb6sU

But a lot of the launch specific data from the day before testing is now no longer valid as the strip is now a lot gripper as there is more and more rubber being laid down on it.
Start getting there but the stress of it counting and the time slipping away take it's tole and I just cannot get a clean run. A couple of people point out that I could score points easy in the high speed. I think at this point I had matched a 9.95 quarter time same as the test day - there was a head wind so despite mid boost rather than low with the odd mistake it should have still been quicker.
So I line up to do a flyer and managed 180mph putting me in the points straight away and manage a faster quarter time of 9.82 on that run. Do another flyer and hold it in 5th longer this time and am happy to see joint 5th at 183.7mph and again a faster quarter of 9.75 @ 149mph which is a new PB for me, despite clipping the limiter in 3rd. Was planning to do another and try and miss the limiter in 3rd when Ian pointed out the smoke on the high speed runs is the rear tyres expanding and touching the bumper and I now have two deep groves in the rear tyres so no point risking it. I should have been running my other wheels for flyers as the drag tyres swell about two inches at 150mph lol but then I wouldn't have go the quicker quarter times. No time left to swap them so day over.
So a very pleasing weekend and I believe I came 10th overall too.
9.75@149 and the 183.7mph
https://www.youtube.com/watch?v=oh_bGte0SX4
incar
https://www.youtube.com/watch?v=kp0SoFQQO8Y

Roll on next year smile

Simon

JollyGrnMonster

Original Poster:

887 posts

198 months

Monday 15th September 2014
quotequote all
I have spent a bit more time than I expected over the past few weeks doing little jobs on the car that look like they shouldn't take long to do but take far longer than expected. Some have been on the list to do for ages and some are required to get to msa regs.

Kill switch and fire pulls added


Pulls added to centre panel also


Nozzles for fire ext added to bulkhead


Msa approved and in date seat and harnesses added


The fibreglass boot lid has never been right since the paint shop painted it the wrong colour and put it in the oven and warped it. So most unlike me I have added a little weight to the car..by using a steel boot lid. This has allowed my current budget of zero to be spent on aero to be used, no fancy wind tunnel or even a trip to b&q required


Mental note to self - remove the totb stickers ASAP after totb.


Simon

JollyGrnMonster

Original Poster:

887 posts

198 months

Thursday 9th October 2014
quotequote all
I spent a bit of time on the car today.

New aim mxg dash installed


Started installing the syvecs paddle shift setup



Easy bit of the shifter setup installed lol