Mac#1 Motorsport Worx Build

Mac#1 Motorsport Worx Build

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Red16

Original Poster:

589 posts

168 months

Saturday 3rd August 2013
quotequote all
Here's the new GT3071R turbo CHRA and ported compressor cover which arrived yesterday







Last night I removed the old turbo ready to strip and fit the turbine housing to this new core.

TheAlastair34

369 posts

128 months

Saturday 3rd August 2013
quotequote all
Red16 said:
Thanks very much for following the cars progress.

Do you have a build thread on your car? I'd be interested to see it if you do.
best one here,

http://www.zsoc.com/showthread.php?t=129613&hi...

98 pages though sorry

Red16

Original Poster:

589 posts

168 months

Saturday 3rd August 2013
quotequote all
TheAlastair34 said:
best one here,

http://www.zsoc.com/showthread.php?t=129613&hi...

98 pages though sorry
Great stuff, i'll have a read through that tomorrow morning with a cuppa smile

Red16

Original Poster:

589 posts

168 months

Saturday 3rd August 2013
quotequote all
This afternoon I removed the turbine housing from my old turbo and gave it a clean up, here it is alongside the new GT3071R assembly



The up pipe from the old turbo compressor housing was cut off and cleaned up ready for welding to the new compressor housing.

Here's the new GT3071R, the old GT3076R and the up pipe



I didn't take anymore photos today, but in a nutshell the turbo has been refitted, along with the exhaust, coolant hoses and oil hoses after priming the turbo with oil.

Red16

Original Poster:

589 posts

168 months

Saturday 10th August 2013
quotequote all
Sorted out an external exhaust today to help with the issue of stinking of fumes after every drive of the car, test drive proved it works :-) a lot quieter at idle but not too different at full chat.






Coskev

80 posts

213 months

Saturday 3rd January 2015
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What's the score with this car now?

Any updates please smile

johneturbo

113 posts

152 months

Thursday 8th January 2015
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I remember this build
I hope he got the issues sorted. He put a lot of effort into the car.

MrWillfin

295 posts

178 months

Tuesday 7th April 2015
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Yes he has indeed, and teh car still lives redface)

He's a friend of mine, current status of the car is that it has a knocking big end bearing.

I don't think he'd mind me saying this, but in the 5 years since the build, the running gear side of things has been a nightmare. Leaking exhaust manifold, then worn piston rings, now big ends.

He's on with a house extension now, but I believe he will give the car another going over this year!

Coskev

80 posts

213 months

Wednesday 8th April 2015
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Good to hear!!

Tell him to update this when he gets time please smile

Mgd_uk

369 posts

104 months

Sunday 27th December 2015
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Any progress on this? smile

Coskev

80 posts

213 months

Thursday 31st March 2016
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His house extension must have been a bigger job than planned!! biggrin

Red16

Original Poster:

589 posts

168 months

Monday 25th April 2016
quotequote all
Update coming very soon... I promise yes

Red16

Original Poster:

589 posts

168 months

Thursday 28th April 2016
quotequote all
Here's a little update on why the car has taken so long to get sorted.

With the house extension plans for the rear ground floor and front garage extension approved building work commenced.



The external shell built up at the rear of the house



This wall needed to come out and a supporting beam installed



Wall removed





Fish tank stand built and installed



Fish tank built on site



Kitchen arrived in millions of boxes and filled the front garage extension



Old kitchen removed and the room plastered



The finished fish tank wall



And the full kitchen



Garage was in a right state and certainly needed a good clear out!



Clearing stuff out made the garage look so much better and actually helped me relax a bit, it was awful seeing the place in such a state!


Red16

Original Poster:

589 posts

168 months

Wednesday 4th May 2016
quotequote all
Right then... I finally found time to get around to looking into the issue with the cars engine, it was running on three cylinders.

Compression testing the engine returned the following results

Cyl 1 = 140bar
Cyl 2 = 140bar
Cyl 3 = 140bar
Cyl 4 = 0bar

Which was certainly worrying!

The car wasn't smoking (aside from the unburnt fuel), pressurising the cooling system etc, externally everything appeared ok, so the engine needed to come apart.



Engine out



Manifolds off, couldn't tell anything looking down the inlet or exhaust ports



Even with the head off there wasn't much evidence to see, looking at the combustion chambers on the head the valves/seats all looked to be in good condition and not bent/damaged, but the pistons crowns had slight marks in the valve cutouts, indicating there had been piston to valve contact.



Removing the cam followers revealed an issue on cylinder number 4, one inlet valve and one exhaust valve had collets out of position, presumably caused when the piston to valve contact happened.



All of the valves were removed, inspected and found to be straight (surprisingly), they were then lapped in, cleaned up and the head reassembled. WD40 poured into the ports and left, no leaks observed so it was cleaned up ready to be installed.

The head was then installed using a 0.027" Cometic MLS head gasket, same thickness as standard Kawasaki gasket.

The cams were installed, timing set and valve clearances checked, all within spec so no need for further adjustments.



Engine back in the car, ready for the final pieces of work to be done prior to getting the engine started up.


Yazza54

18,508 posts

181 months

Wednesday 4th May 2016
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Is that new gasket thicker than what you were running before then?

Red16

Original Poster:

589 posts

168 months

Wednesday 4th May 2016
quotequote all
Yazza54 said:
Is that new gasket thicker than what you were running before then?
Unfortunately I can't say, I can't find any evidence of which gasket I bought and fitted last time, I know it was a Cometic MLS one but they do 3 different thicknesses, I tried measuring the old one but didn't get a definite reading, a thinner gasket last time could possibly account for the piston to valve contact.

Yazza54

18,508 posts

181 months

Thursday 5th May 2016
quotequote all
Red16 said:
Yazza54 said:
Is that new gasket thicker than what you were running before then?
Unfortunately I can't say, I can't find any evidence of which gasket I bought and fitted last time, I know it was a Cometic MLS one but they do 3 different thicknesses, I tried measuring the old one but didn't get a definite reading, a thinner gasket last time could possibly account for the piston to valve contact.
Yeah, good news you got away without scrapping a piston or valve but it's always nice to know the absolute reason a problem like this occurred, think I would have been re fitting with the thickest I could find!

sparkyj83

14 posts

123 months

Monday 9th May 2016
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Glad to see this monster is getting back together it was my main build gide for my mac1

Coskev

80 posts

213 months

Sunday 19th June 2016
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Great to see an update smile

Will it be on the road this summer?


Red16

Original Poster:

589 posts

168 months

Thursday 4th August 2016
quotequote all
Yazza54 said:
Red16 said:
Yazza54 said:
Is that new gasket thicker than what you were running before then?
Unfortunately I can't say, I can't find any evidence of which gasket I bought and fitted last time, I know it was a Cometic MLS one but they do 3 different thicknesses, I tried measuring the old one but didn't get a definite reading, a thinner gasket last time could possibly account for the piston to valve contact.
Yeah, good news you got away without scrapping a piston or valve but it's always nice to know the absolute reason a problem like this occurred, think I would have been re fitting with the thickest I could find!
I think the piston to valve contact was caused by it being over revved. Having not used the car in literally years, I forgot there was a switch to turn the Flatshifter Expert kit off, meaning full throttle gear changes were carried out without ant ignition cut at all, that is where I think the issue has came from.