What's happening in your garage this weekend ?

What's happening in your garage this weekend ?

Author
Discussion

adam quantrill

11,538 posts

242 months

Monday 3rd July 2017
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Mostly cleaning, more cleaning, polishing, buffing.... and check the fluids.

batman400

1,486 posts

204 months

Wednesday 5th July 2017
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With the fest fast approaching......

The alternator mounting bracket needed the top right bolt replacing with a countersunk one of the correct size as it fouled on the alternator plastic cover. It's still tight but the cover has enough "give". Oddly when I took the mount off the same bolt was stuck in the head with RTV !! it looks like Rover changed the thread size in the head so when the Chim engine was fitted the bolt was too small so rather then drill the hole in the bracket out and fit the correct item they reached for the Silicone Gun !! The existing wiring has been left in the loom (so the mod can be reversed) but made safe and two new 8mm battery cables run in via 100A fuse but the Positive battery terminal needed a longer bolt as there a now a number of additional connections !



Needs a small spacer piece between the alternator rear mounting and the bracket as it's just loose on the studding at the moment.



Test's look good, with a DVM connected across the battery it's maintaining 14v even with Heater, Headlights, Driving lights and rad fan running and no more burning rubber !!

Jobs left : Fit bonnet, drain a bit of oil out as I've overfilled it Doh and give her a quick wash !!

Another thumbup to the guys in the Drawing office and Mech workshop where I work

eesbad

1,329 posts

202 months

Saturday 22nd July 2017
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Just replaced the heater hose that failed on the way back from BBWF. That 30 year old hose really didn't want to come off! All done now though.

rev-erend

Original Poster:

21,408 posts

284 months

Saturday 22nd July 2017
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What about the plenum thermal insulator ?

Alan461

853 posts

131 months

Saturday 22nd July 2017
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All day in the garage having fun.
Took the manifolds off for blasting and painting.
Bit more work on the suspension etc.

eesbad

1,329 posts

202 months

Sunday 23rd July 2017
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rev-erend said:
What about the plenum thermal insulator ?
I'll do that when I swap out the other heater hose. Just wanted to get it back on the road for a run before we go on hols this week!

billynobrakes

2,675 posts

265 months

Sunday 23rd July 2017
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I really went to town

Put an Ali gear knob stop on, looks a lot better now as you cant see the black gear shaft smile

Took the round black plastic mobile phone holder off the dash and that looks better as well wink

Still messing about with the settings on the shocks but cant get a good compromise either too hard or too soft so definitely needs a trip to Gaz for monotubes

adam quantrill

11,538 posts

242 months

Sunday 17th September 2017
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Replaced the offside front wheel bearing and a quick test drive showed the noise has disappeared.
If looked like the inner race rollers had stopped rotating freely, but it wan't too worn.

Did sone fettling of the nearside outrigger and noticed a crack in the exhaust manifold so that was welded and sounds a lot quieter.


v8s4me

7,240 posts

219 months

Monday 18th September 2017
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NOTHING! It's almost finished and MOT booked for Saturday biggrin

mk1fan

10,516 posts

225 months

Monday 18th September 2017
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Think I've traced the running fault to a failed CTS. Part ordered along with appropriate deep socket. Will swap out when delivered, hopefully tomorrow.

eesbad

1,329 posts

202 months

Monday 18th September 2017
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mk1fan said:
Think I've traced the running fault to a failed CTS. Part ordered along with appropriate deep socket. Will swap out when delivered, hopefully tomorrow.
Annoyingly, I had a brand new one in the boot when I was with you in Greenwich, Saturday before last... Hopefully this will sort it!

mk1fan

10,516 posts

225 months

Monday 18th September 2017
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I have a spare already - but have ordered a second with part number in the 'Parts List' sticky. Wish I had fitted it when I had all the upper plenum stuff off the car!

I can't find a spec comparrison for the two different parts numbers BUT have found a working temp range for the parts list one that is 25-80 degrees. Clearly a bit low!

I also found that I can test check with a 200Ohm resistor - I go past Maplins every day - if the deep socket doesn't turn up in a timely manner.

Thanks.

adam quantrill

11,538 posts

242 months

Tuesday 19th September 2017
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You might find that the socket doesn't fit over the connector. I always use a spanner. Possibly 17mm?

mk1fan

10,516 posts

225 months

Tuesday 19th September 2017
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Impact socket doesn't fit because the plug gets in the way. A 12 point socket should fit.

Tested the circuit today using a 200 Ohm resister. All the running issues dissaappered so I'm fairly confident I found the problem.

Just waiting on the socket. Tomorrow night looks good to get her sorted.

eesbad

1,329 posts

202 months

Wednesday 20th September 2017
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mk1fan said:
Impact socket doesn't fit because the plug gets in the way. A 12 point socket should fit.

Tested the circuit today using a 200 Ohm resister. All the running issues dissaappered so I'm fairly confident I found the problem.

Just waiting on the socket. Tomorrow night looks good to get her sorted.
Fingers crossed!!

mk1fan

10,516 posts

225 months

Wednesday 20th September 2017
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CTS changed. Running fine now.

Slightly more involved than I had hoped. The deep socket was 5mm too long and the vac pipe was in the way. So a bit more strip down than had hoped. Started at 7pm. Finished at 8pm incrunning her up to temp. No leaks as yet but will check again after a run.

Booked in to BD Engineering on Tuesday for a rolling road tune and to have a look at the dizzy oreintation which seems to be 90 deg out.

eesbad

1,329 posts

202 months

Wednesday 20th September 2017
quotequote all
mk1fan said:
CTS changed. Running fine now.

Slightly more involved than I had hoped. The deep socket was 5mm too long and the vac pipe was in the way. So a bit more strip down than had hoped. Started at 7pm. Finished at 8pm incrunning her up to temp. No leaks as yet but will check again after a run.

Booked in to BD Engineering on Tuesday for a rolling road tune and to have a look at the dizzy oreintation which seems to be 90 deg out.
thumbup


adam quantrill

11,538 posts

242 months

Saturday 30th September 2017
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Fettling the offside outrigger which is a bit of a pain as the fuel lines have to be moved out the way first. What a rust trap that area is! Now it's less like swiss cheese and reasonably solid. I have a plan to replace both sides fully but with stainless, that way the dry bits out of range of the engine oil will be impervious to future failures.

If any of you have not replaced your outriggers on SE style bodies yet, I would recommend drilling a small hole (4-6mm or so) in the side of each one about half way down, and then squirting some oitl in, as they appear to corrode from the inside out as well as the outside in....

Also decided to do the nearside front bearing which I did before only 2 years ago but it's also whirring a bit, so I must have made some small error when I did it last.

Finally I have a rear driveshaft UJ ready to go on if needed as I am hearing a clonk from the rear.


KKson

3,403 posts

125 months

Saturday 30th September 2017
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Wedge work entailed washing and polishing the black Wedge. Driving there and back to the Neil Garner Open day, getting the car literally covered in cow st after being stuck behind a cattle truck for several miles and then washing and hosing it yet again.

batman400

1,486 posts

204 months

Monday 2nd October 2017
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Busy finishing the garage lining...

Then testing an old Dyson pretty much to destruction (Note filters clog in 6min not 6months...)



Then moved the wedge in !