Stuart Twin Victoria (Princess Royal) Mill Engine

Stuart Twin Victoria (Princess Royal) Mill Engine

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dr_gn

Original Poster:

16,181 posts

185 months

Saturday 9th July 2022
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MKnight702 said:
dr_gn said:
Might not look much at the moment, but there is a lot of work just in those assemblies…
That's a slight understatement of the work you have done. If I had a quarter of the skills you have I would be a very happy man.
Thanks very much - I’m happy with it so far, but what I mean is that for example the beds and cylinders now just look like single lumps of metal (which is how they should), but in reality they are made of dozens of bits of metal, machined, stuck, bolted and filled to look like castings. So half the work that’s gone into it is invisible…

dr_gn

Original Poster:

16,181 posts

185 months

Saturday 9th July 2022
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dudleybloke said:
Looking very nice indeed.
I've never used a mill smaller than a Bridgeport but I've used a few shonky ones and know what you're going through with regards to machine limitations.
You are doing a superb job with what you've got and seem to have picked up the feel of it pretty quickly.
Thanks - both the lathe and the mill have their foibles, but I guess compensating of them is just part of the process.

dr_gn

Original Poster:

16,181 posts

185 months

Sunday 24th July 2022
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Bit of an annoying setback with this. I started on the main bearings, which I bought as gunmetal castings:



But it turns out there was a design change in the distant past, which means that they aren'r really suitable for this engine (too tall, plus the boss width is short on mine).

So, with some advice from the ME forum, I opted to make them from scratch out of aluminium, with separate split brass bearings. So I made a start:





Everything went fine up to the point of bolting the halves together, when I found that there was on overlap of the cap bolts. I thought I'd machined it wrong, but basically if you make one bolt face right, the others (lowers) wont fit:



You can see the overhang here:





Turns out that there is a thing called "one size smaller" for BA fasteners, that means that, say, you can have a 5BA bolt, with a 6BA head:



It also turned out that the lower nuts I'd got were oversized, and if I'd had the correct ones, everything would have - only just - fitted.

Anyway, I opted to scrap the half built ones, draw new ones out on CAD, and do my own drawings. I've added some radii featuures to add a bit of bulk, and tweaked the stud centres to give more room:







So I'll try again...at least only half finised one of them.


dr_gn

Original Poster:

16,181 posts

185 months

Sunday 21st August 2022
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So, started again with the housings, a repeat of the previous process with a few minor tweaks for the additional radii:







I made a spigot to do the O/D, which worked well enough:





I also left the 1mm oil hole until after boring, because last time it caused a flaw when boring the hole:



Milled a pocket for the oiler bosses:



JB welded in place:



And a Milliput “rolling ball” fillet - far more satisfying than in CAD:



Currently awaiting primer:



Next, the crankshaft I guess.

dr_gn

Original Poster:

16,181 posts

185 months

Sunday 28th August 2022
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anonymous said:
[redacted]
I rebuilt my old Revell "Visible V8" recently (with a few refinements) - I'm happy with just having that as a cutaway!

dr_gn

Original Poster:

16,181 posts

185 months

Sunday 28th August 2022
quotequote all
On to the split main bearings.

Hacksawed some square section brass bar into radius sized pieces:



Milled them square:



Tinned and sweated them together:





Them milled the assembly to clean-up the sides:



Centre drilled ready for fitting in the 4-jaw chuck ready for boring to crank journal size. Have to make the crankshaft first though:




dr_gn

Original Poster:

16,181 posts

185 months

Monday 5th September 2022
quotequote all
After much frustration and faffing with poor surface finish (turned out the material I was using was the wrong grade of steel- 080A15 vs. EN1A), finally made a start on the crankshaft:



Opted to do it in two stages - roughing and finishing. Roughing done in the chuck:







So far so good:



Finishing next, which will be done between centres (hence the centre drillings). Then I can use the shaft as a plug gauge for the split main bearings, cast crank webs, flywheel, eccentrics and governor pulley.

dr_gn

Original Poster:

16,181 posts

185 months

Tuesday 6th September 2022
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Spent ages adjusting the set-over of the tailstock, with it locked in place longitudinally, ready for turning the shaft. Managed to get it to zero on the calipers, turned out to be 0.0002” diameter difference with the micrometer. That’s over about 3.6”:



Hopefully that will be good enough because it got the stage of fractions of a turn tightening or loosening one adjuster shifted it from + to - size.

Also made an aluminium split sleeve to protect the steel shaft from the carrier:



Found a neodymium magnet to hold the carrier to the drive peg. I’m sure there’s a more traditional method, but this worked fine - held it together while turning, but allowed the work to be removed easily too:





Runout on the turned parts is on average about 0.002”, easily lost in the excess material:



On to the axial error caused by the centre drillings, this was about 0.001”:



Might double-check the tailstock setting, then get in with finish turning the shaft next time.

dr_gn

Original Poster:

16,181 posts

185 months

Wednesday 7th September 2022
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Thanks Rolster, yes the quill was locked for all readings.

dr_gn

Original Poster:

16,181 posts

185 months

Thursday 8th September 2022
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Turned the shaft between centres using slip gauges to get consistent lengths both sides. Also used the same final diameter tool setting and swapped ends to ensure identical diameters end-to-end:





The result was 3 out of 3 diameters were identical to within the 0.0005” resolution of my digital calipers. I then switched to my micrometer 0.0001” resolution which showed 1 out of the 3 diameters to be identical, the remaining two were 0.0002” different.



This is after finishing with fine abrasive. I’ve left 0.25mm on the ends (as per instructions), so the centre drillings will end up a bit smaller.

dr_gn

Original Poster:

16,181 posts

185 months

Friday 9th September 2022
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alleggeria said:
What is the importance of having both sides of the shaft within such tight diameter tolerance relative to each other? You could also turn both sides and then adjust the bearings accordingly or am I missing something?
There is no reason other than if it’s easy to get it right, why not get it right?

Folks on the ME forum seem mildly outraged by my method of using the same tool settings for each end of the work (and swapping the work around in sequence), despite it clearly giving a more consistent end result than finishing one end, then doing the other (at least for someone of my limited experience).

Say I finish one end, then measure, cut, measure, cut the other until I end up needing, say 0.0007” to get to the same as the other end. How am I supposed to take that cut accurately when my slide dial is graduated at 0.001”? In some cases the top slide can be angled to make one graduation effectively less (calculated using trig), but that then messes up the length stop distances. Far easier to do it as I have done (in my opinion).

They just say “that’s not how it should be done”, yet I don’t remember any technical reason being given as to why that’s the case…Maybe I misunderstood something or other, but the micrometer doesn’t lie, and the maximum error I’ve ended up end-to-end over the three pairs of diameters is 0.0002” (that’s about 5 microns). One of the pairs is bang on the same to the resolution of my micrometer, which is 0.0001” (about 2.5 microns).


dr_gn

Original Poster:

16,181 posts

185 months

Sunday 23rd October 2022
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Made a start on the split main bearings.

Centred the brass block:



Drilled to 10mm so I could a) get a boring bar in, and b) give clearance for the crank spigot so I could test fit the crank shaft all the way along it’s journal:



Faced off to form a thrust face:



Then bored to a tight running fit on the crank:



Then took intermittent cuts on the square to form the o/ds of the bearing side faces:





Unfortunately this partially broke the solder joint; when I test fitted the crank again, oil slowly bubbled out of the joint.

Anyway, thought I might as well carry on, so formed the bearing holder groove with a parting blade - deeper cuts at each end:



Test fitted until the halves just about closed:



It fell apart after final parting, but after cleaning the faces it looked fine:











There is a bit of a gap left when the cap is screwed down to a good running fit. If fully tightened it gets a bit too tight for comfort. I expect once it’s been lapped in it’ll be spot-on:



The parted-off face needs thinning a bit, but I can do that with wet & dry on the surface plate.

I did make a mistake and over-bored a bit of the block at first, but hopefully I’ve got enough left to clamp in the chuck and make the other. Anyway, so far so good.

dr_gn

Original Poster:

16,181 posts

185 months

Monday 24th October 2022
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rolster said:
Hi there it looks to be coming along nicely and as it runs in it should settle down nicely.

Be careful of lapping (choice of lapping compound especially) the bushings as the grits may imbed in the bushing giving an undesired effect when running.

I would not be to worried about some of the comments on the ME forum. Almost all are made in a effort to pass on some form of help, but i feel some on the forum are regimented into the way they were taught themselves and don't see that there are always more than one way to acomplish a job, despite them having many years of machining expirience. Some of the more experienced people there, have a selection of tools assembled over a lifetime of machining, the likes of which us mear mortals would only dream of and so they sometimes forget we dont have the same selection to draw on.

At the end of the day its your project and you make it how you want to and enjoy the process as its supposed to be about enjoyment not a chore of work, like that Aero Vulcan! wink
Thanks Rolster. Yes, all good, the shaft machining worked in the end. I asked a couple of other machinists at work, and that said they’d do it like I did, so I’m fine with it.

For lapping I think Autosol and oil would be enough. I’m going to leave that until the whole thing is set up on its base so that it’ll lap in when it’s in its final alignment.

dr_gn

Original Poster:

16,181 posts

185 months

Saturday 29th October 2022
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I was pondering why the brass bearings had been so easy to turn to be a perfect fit, simultaneously in both the housings and to the shaft, as well as side-to-side in the housings. With my skills I knew it was very unlikely to achieve such a good fit straight away.

After some measurement I found that the o/d of the bearing groove was smaller than the I/d of the housing, yet it seemed a great fit, with no play either up or down or side-to-side.

Careful examination revealed the inevitable error: the parting tool I used for grooving had been ground to a slight taper, and therefore the insides of the groove flanges were also tapered. So when the bearings were ‘near enough’, light pressure deformed the housings enough to give the impression of a perfect, snug fit:



However, pressing the bearings fully home with a plastic pen showed the true situation - a gap, and a loose fit to the shaft:



Of course all might be well initially, but any radial load on the shaft (e.g. imperfect flywheel/crankshaft balance) would eventually displace a bearing, with a resulting death rattle on the engine.

Metal shims are out, due to oil needing to flow vertically into the top bearing half with no leakage path between the bearing and housing. Liquid shim is ruled out because it has no place in a precision bearing fit on a steam engine. So unfortunately the only remedy is to scrap all the bearings and start all over again from raw square brass bar as per 28th August.

Lesson learned: check equipment, and for me - stick with my rule of never using HSS tools unless there’s no other option.

dr_gn

Original Poster:

16,181 posts

185 months

Tuesday 7th March 2023
quotequote all
So after getting a bit demoralised over the bearing error after all that work (about 6 months ago - time flies) this evening I started again from scratch: cut the new brass bar to approximate size with the hacksaw:



Then milled the mating faces and their opposites to the same thickness:



Now ready to solder together again, then final milling of the flanks and ends:



Hopefully I can get the solder to work a bit better this time too.

dr_gn

Original Poster:

16,181 posts

185 months

Wednesday 8th March 2023
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Soldered the bars together, milled them square and centre drilled them. Then back into the 4-jaw chuck ready for some action with my shiny new (non-tapered) grooving tool:









Ironic I was waiting for warmer weather, and now it’s colder in the garage than ever.

dr_gn

Original Poster:

16,181 posts

185 months

Thursday 9th March 2023
quotequote all
So, deep breath, and try again…

I cut the block in half to stiffen everything up:



Faced:



Flange O/D turned from square:



Set the grooving tool normal:



I had to use back-gear to avoid chatter, but all ok. The recess was by far the hardest part. Once again I found it difficult to judge dimensions and simultaneously machine a width and diameter without going over or undersize on one or the other. Having the saddle stop at one end was fine, but it’s fresh air at the other end, and very easy to go too far in the width while getting the diameter. What I did was get the width right, then when the diameter was almost there, undersize each end to avoid the pedestal radii. This left a raised block in the middle, and I changed tools to a normal turning tool to reduce that until it was the perfect diameter to match the housing. All a bit sketchy I think, but it worked.

Then clamped in the spare housing:



Drilled and bored to a good running fit on the shaft:



Then parted-off without issue. Again, judging and adjusting the cut to give the right flange dimension was very difficult:




Here’s the result:













Fit seems fine, runs smoothly enough with the cap screws loosely tightened, but binds slightly when fully tightened.

So I’m calling that one OK. Now for the other side.

dr_gn

Original Poster:

16,181 posts

185 months

Friday 10th March 2023
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Got the other bearing made, so far so good:












dr_gn

Original Poster:

16,181 posts

185 months

Friday 10th March 2023
quotequote all
dudleybloke said:
Looking great.
Thanks DB.

dr_gn

Original Poster:

16,181 posts

185 months

Saturday 11th March 2023
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AlfaCool said:
Well spun up Doc.
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